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 "Bankamericar"
AA/FD Restoration
- Page 3 (Cacklefest
2003 - Not How We Planned It)
Wednesday,
October 01 started off with high expectations. The car was finally
done and ready for its maiden fire-up. The plan was to get the
fuel system close, check for leaks and put her in the box for
the weekend. Wrong! At the foot of John's driveway a very bad
thing happened. After the first fire-up that produced a high
idle, the car was shut off, adjusted, backed off and then refired
- not! As soon as John hit the mag switch there was a huge "boom"
and the street was littered with scrap metal and block fill!
Seems the block was not magnafluxed or ultrasounded before the
machine work was done and the autopsy revealed that there were
minute cracks in the # 2 and # 4 cylinder walls. Nitro got in
them after the first fire up and when they got spark on the second
- done deal.
Needless
to say it was a very big let down, especially after all the hard
work it took to get the car done for the CHRR. With no spare
parts whatsoever it looked like our weekend was trashed. I was
driving down from Oregon and crossing the Siskiyous when I got
the news and almost drove off the road. Like the others I was
shocked and really bummed! I thought for awhile and called John
back and told him to put it in the box and come to Bakersfield
- we'd figure out something.
 First fire up was fat and fast idle.
 After the boom John
gets out and looks down at the damage. Pieces hit Crew Chief,
Ronnie Rapp in the food and cut Alex Mikkelsen's legs.
 1000 words..........
 The explosion was so
violent it pushed the upper fraim rail out 4" at the motor
mount and put dents and a hole in the freshly painted body panel.
Ouch!
 Out
of the box on Thursday afternoon.
Fast
forward to Friday morning. We had stopped licking our wounds
and got into drag racer mode. We spent all day Thursday looking
for a 392 fuel short block to borrow or buy with no success.
Late Thursday we finally got lucky when Don Green (Rat Trap)
offered his spare Donovan long block. Although it was not period
correct, it was the only option we had. And so "The Great
Cacklefest Thrash of 2003" began.
 The body was stripped
and the car was ready to go on the stands for the swap.
 Getting the dead 392
out was no problem.
 Again - 1000 words ......
 Once the 392 was out
all the parts were laid out to go on the Donovan. Ya gotta love
our huge hi-tech work bench. It was suppose to be our picnic
table!
 After pulling the long
block out of Green's truck we started figuring out what we needed
to make it work in our car. A car that was built in 1968 and
NOT designed for a Donovan. As it turned out, there were a lot
of parts we needed to make this deal work!
 Alex and Don Green put our degree wheel on the
engine.
 By Friday
afternoon, after finding and changing the stepped bellhousing
studs we needed (thanks to Jon Halstead) we were ready to drop
the Donovan in and see what we were facing to make it fit.
 There were three major
problems. One, the ribs on the Donovan wouldn't allow it to sit
properly in the frame rails. Two, the oil pan was to deep and
three, the oil filer assembly wouldn't fit at all.
As day
turned to night we'd spent most of the afternoon scrounging parts.
I can't even remember all the little stuff we needed like lash
caps (thanks Gene Amaya), a brass oil pump drive (thanks Don
McManus), a line up shaft (thanks WW2 Racing), assorted nuts,
bolts and aluminum grinder (thanks Jack Harris), 1/2" pitch
blower belt (thanks Dennis Fenstermaker & Brendan Murry),
oil (thanks Frank Genco), generator & compressor (thanks
Dennis Prater) and the biggie - special thanks to Darrell Tedford
(Tedford & McGee) for bringing this from home -- the only
shallow oil pan that would work on the car! That's what brought
it together. And then there was Tom Hanna's crew that cut the
baffles out to make clearance for the 5/8" stroker. This
was definitely a group effort!
 After
we got the pan, the oil pump had to be changed (out of our old
engine) and gaskets had to be made. Chuck Goebel is just one
of the racers who stepped in to help over the ordeal.
 The biggest
task by far was grinding the ribs on the block to fit in the
chassis. Bob Damly and Rick Kepler did all the grinding with
a hand grinder and small compressor -- it was a laborious job
that took about 2 hours.
 As the block was prepped,
everybody else made sure the other parts we needed were ready.
Bob Danly
and John Jennings made the on-site custom parts needed for the
engine to finally fit.
 By 10 PM we were ready
to drop it in again.
 Bingo! After all the
alterations it was a perfect fit.
 Ronnie Rapp and Bruce
Dyda install the clutch - she's almost done. We then installed
the bellhousing, steering and linkage and called it a night.
 Finally - the Donovan
is in place waiting for plugs and fuel.
 Saturday
morning we put the top end on and by 10 AM were ready for another
first fire-up.
 A collective
sigh of relief and high fives followed as oil pressure came up
and the engine fired. It was fat but that could be fixed....and
we had some oil leaks and those were also fixed.
 Putting
the cowl on was the last step before the second fire-up.
 After
a major change in the fuel system we were ready to try her again.
This time we gave the seat honors to Lynn Kane who, back in April
of 2003, was the first fan to step up and offer parts for the
restoration. His help has been overwhelming and nobody deserved
the second fire-up than him.
 Alex raps the throttle
as Lynn enjoys the moment.
 I
told him he'd need ear plugs! After the fuel system fix this
baby was pounding the ground.
 Lynn described the experience
as a "life highlight". We're sure glad we could give
it to him.
 Our
next step was to get everyone in sync for the Cacklefest push
start. John hadn't push started a car since the 1970 March Meet
and it had been 33 years (1975) since I was push started. In
spite of suffering from a gallbladder attack that had plagued
me since the previous Thursday, I was strapped in the old girl
for the first time since 1971... and I was in heaven.
 Once
we made the turn onto the strip it was 1971 again. It was magic
- like we were all young again and this was something we did
every weekend. John did perfect and the car fired right up. What
a friggin' thrill! Needless to say, everyone who had busted their
butts the past two days were ecstatic. We'd pulled off the improbable,
if not the impossible.
 Getting
lots of looks was John's '58 Chevy built by John Jennings at
Outlaw Products...and it had the trickest push bar ever.
 After the car fired
I took it past the lights and stopped so Ronnie could give the
engine a once over. She was clean and dry.
 Back to the pits
We were ready for
Cacklefest!
 On Sunday
morning we got a very unexpected surprise - a shock actually
- icing on the cake. At 10:30 we were informed that they needed
the car, push car and crew on the starting line in 20 minutes.
Seems the staff had unanimously voted us the car that best represented
the era and the overall spirit of Cacklefest.
 Dave McClelland interviews John Ewald about
the car - its history/restoration and what we had to go through
to make the call for Cacklefest.
 The
core crew Alex Mikkelsen, Ronnie Rapp, John Ewald and Don Ewald.
 John, Gregg Sharp and the dumb driver (ask any
owner, all drivers are dumb! LOL).
 More of the gang: Alex Mikkelsen, Rick Kepler,
Bruce Dyda (who did the restoration) Ronnie Rapp (Crew Chief),
Greg Sharp, John & Don Ewald.
 Jim MacMonagle does an interview for 1010TV
 Back in the pits we had to share the award with
the guys who made it possible - Don Green and Ron Hope.
The rest of our day was
spent taking Don's engine back out and putting our dead player
back in. Was it worth it? One and all say "ABSOLUTELY"!
This was not something any of us want to go through again (and
we won't) but what a great story for a bunch of old dogs who
though their thrashing days were long over. Next time we'll be
more than ready and are looking forward to many more CHRRs to
come.
Again - many thanks to
EVERYONE who made this happen.
UPDATE
12-11-03
 Update time for the "rebuilding
of the rebuilt BankAmericar". Bruce Dyda has repaired the
frame rail and engine mounts (which had been pushed out 4 inches),
and he kept the fix behind the body panel so it will never show.
He is good at what he does! He also redid the brake system and
the clutch... figured we didn't need the counter weights and
all those springs... Don's leg was getting a bit tired in the
Cacklefest until Ronnie got the clutch pin in. Thanks to Weber/McLeod
clutches for doing the final balance. We now have a good block
to work with thanks to Dennis Fenstermaker and Ken Rappaport
of Race Car Research. Henry Velasco straightened the crank, Jerry
Sweeney at Brooks Rods fixed the one hurt rod and Arias knocked
out a new piston. Gene Mooneyham checked the blower and confirmed
it was not hurt. Our best fan Lynn Kane came up with a NOS set
of gaskets for everything... don't know where the hell he finds
all this stuff! But I sure am glad he does. In this first shot
is the repaired rails. JE
 Being the owner of a
top fuel car has it's drawbacks... like having to deal with a
crew chief by the name of "Sir Ronnie" Rapp. He has
this very weird way of making me greet him...
 For those of you that think Ronnie is
just a grump with no since of humor...you haven't spent time
with him. He even cracks himself up working on the injectors.
 Forgot to mention above... the heads
were fixed and made all better by Larry Ofrea at Valley Head
Service. Glad Ronnie doesn't mind that drive to his shop from
Orange County... took him about 3 hours each way <grin>
JE
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